◂ AppsGTS Exec SuiteGTS Exec

W.A. Parish U8 — 7FA Major Inspection

GTS-2022-014CLOSED 5/16/2022
Edit
Added Jun 18, 2026Completed Feb 25, 2022
Company
Gulf Turbine Services
Client
NRG Energy
Source
MANUAL
Contract Type
T AND M
Market Segment
GT_OUTAGE
Public/Private
PRIVATE
Project Manager
Ray Daniels
Estimator
Phil Carter
Superintendent
Joe Tibbetts
Location
Thompsons, TX

Margin Analysis

Original Margin
14.0%
$448,000
Revised Margin
13.8%
$498,000
Final Margin
8.2%
$295,720
Margin Fade (Bid)
-5.8%
CO Impact
$50,000
Margin Fade (Revised)
-5.6%

Where They Land

Final Margin+8.2%
Break Even
-0.9%+24.4%
Gain / Fade-5.6%
As Predicted
-7.9%+2.0%
This project
Other projects
Zero reference

Revenue & Cost Summary

StageRevenueCostProfitMargin
Original$3,200,000$2,752,000$448,00014.0%
Revised$3,610,000$3,112,000$498,00013.8%
Final$3,610,000$3,314,280$295,7208.2%

Cost Category Variance

CategoryOriginalRevisedFinalVariance $Over/Under %
Labor$1,050,556$1,218,552$1,364,778+$146,226+12.0%
Material$774,771$963,198$996,910+$33,712+3.5%
Subcontractor$661,857$840,670$839,675$-995-0.1%
Equipment$252,808$265,722$284,854+$19,132+7.2%
Other$82,560$93,360$84,024$-9,336-10.0%

Labor Productivity

Original Rate
$60/hr
Revised Rate
$69/hr
Final Rate
$72/hr
Hours Variance
1,446
Rate Variance $
$227,461
Volume Variance $
$86,761

Lessons Learned

Borescope found more R1 bucket distress than the planning scope assumed. Added 4 days of disassembly labor. Pre-outage borescope access needs to be a hard gate before we bid the hours.